Before coming home for leave in August 1997, I decided to have some maintenance done at Gran Prix Motorsports. And I forgot to mention, I was also lucky enough to find a used Fox Twin-clicker rear shock when I was home back in March.The Fox Twin Clicker. Manufactured 2/87. Rebuilt in 2002 by Curtis Pell of the now defunct California Suspension Works. This shock eventually made it's way on to my 1986 1100 Roadrace bike.
While I was at Fort Hood, I had the shock rebuilt by Rick Sage of Sage Racing in Denver, CO. Gran-Prix Motorsports handled the installation
along with new steering head bearings, an oil change and a carb clean. Granted, I normally did all of the maintenance and work on my bike,
but I was tired of spending a couple of days prepping the bike each time I went on leave. I finally decided to fork over the dough to get
it done so I could just pick up the bike and ride.
Spring 2002, with the motor and shock removed.
During the next four years, a lot happened in my life. I left the Army, moved to San Antonio, and eventually wound up in Northern California.
I never forgot about my old Suzi, but just didn't have the time nor the space to store and work on her. While in California, I started thinking about
getting the bike back under my wing. I finally had the space to put all of my tools and the bike.
'85 motor just out of the crate.
After much thought I decided against making a "7/11" bike (750 frame, 1100 motor) on advice from a friend and mechanic of mine. He did the conversion, but said that it really affected handling and was really too much torque and power for a frame that was not reinforced. I opted searching for an old complete junkyard motor to drop in the frame.
Spring 2002, on first ride in 4 1/2 years.
While the new motor was being shipped, I pulled the original motor out of the frame, and had the rear shock rebuilt adding a correct rate spring for my weight. I also
bled all the lines with fresh DOT 4 fluid and cleaned the frame.
My favorite fuel intake system. Having uninstalled, rebuilt and reinstalled at least a hundred sets of carburetors, having to remove and install them from an airbox with those fuel hardened boots is no fun. Knowing this, I went ahead and ordered a nice set of new pliable 34mm intake boots.Motor bolted into the bike. Ready to fire up and wake the neighbors.
NOW . . . to start her up. Another gearhead from across the street from me was helping me to drop the motor in and bolt her up. By the time everything was
in and the fuel bottle connected, it was around 11 p.m. My neighbors are pretty forgiving so I figured "What the hell," and pushed the start button. It only
took a couple of cranks and she bumped off! I couldn't believe it. No unwanted noise and running great. I let her run for about 30 seconds, then shut her
down due to the lateness of the hour. The exhaust was a bit smoky, and I wasn't sure what was causing it, but it would have to wait until morning. I connected
the fuel tank, and put some of the plastic back on her.
Classic Yoshimura side cover. After four-and-a-half years, I was dying to ride her. I woke up early, tossed her on the stand and fired her up to see if the smoke would go away. I also wanted to check for oil leaks, and honestly hope she wouldn't "grenade" on me. Most of the smoke cleared up right away. Was most likely from sitting, and the WD-40. I was hoping that was the case. There was still some smoke, but nothing to worry about. There were also a couple of oil leaks. I tightened the covers down more, and it seemed to stop it temporarily. The bike was running fine, and after an idle adjustment, I tossed on the leathers and took her to work.Spring 2002, on first shakedown ride in Nor-Cal. It was immediately apparent that the carbs needed adjusting. BUT, she was running OK for a short jaunt. Another thing I noticed was that the transmission was really sticky while shifting. I thought the clutch might have to be replaced, but at least it was not slipping. It was most likely caused by sitting for so long with no oil in it.The original 1985 motor had 29mm carbs. They were updated to 31mm in 1986, and 34mm in 1987. I had to drop the needles all the way after I installed the carbs. The main jetting was OK. Once I got her off base and on the road, I found she still ran slightly rich and had a wonky flat spot at 4K rpm no matter what adjustments I made. I could have DYNOED her and got her totally sorted but honestly, she ran well enough for me. |